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Every now and then, even solid wrenching experience and high-quality tools fail to remove a firm, determined bolt. Hopefully, the result is only a stripped head and not a broken bolt shaft. Experience lends to knowing when there's enough removal torque being applied to become concerned, stop the attempt and revaluate the situation. I made two good faith attempts to remove a lower shock bolt when I knew any more applied torque would fail and alternative removal measures were going to be needed.
I already had a new replacement bolt and a multitude of bolt extractors, but I have had an idea for a hack for a number of years, but had never had a need to experiment with this technique. With the plan already in place to extract a defiant bolt, I decided I would go for increasing removal torque until it backed out or stripped the head. After applying good standard practices (firm pressure and gently increasing torque), it stripped. Once it started to go, there was no going back. The stripped and removed bolt below.
The hack was to try doubling up some 0.021" Stainless Aircraft Safety Wire and see if it could be placed into the bolt's hex head cavity and have a slightly larger hex head socket drive (8mm to 1/4" hex tool) driven in with a brass hammer to increase the purchase of the hex tool to remove the stubborn stripped bolt.
I bent the safety wire using my needle nose pliers and formed this: (Note...the photo is the replaced bolt because it didn't take a photo before removal attempt. Only shown for wire placement example)
This fitted into the stripped bolt head like this:.
This was a photo of the concept attempt:
Followed by driving the 1/4" inch drive hex socket into the bolt hex head. It worked like a charm. No special tools or extractor required. Below is the actual extracted bolt.
I was a bit amazed at the ease of this hack. It required no special tools and theoretically could be performed in the field provided you could find appropriate wire to complete the task. This took about 30 minutes with some concept wire placements to figure out if this might work. Once I figured out a workable wire placement, it took only a few minutes. Cheers!
I already had a new replacement bolt and a multitude of bolt extractors, but I have had an idea for a hack for a number of years, but had never had a need to experiment with this technique. With the plan already in place to extract a defiant bolt, I decided I would go for increasing removal torque until it backed out or stripped the head. After applying good standard practices (firm pressure and gently increasing torque), it stripped. Once it started to go, there was no going back. The stripped and removed bolt below.
The hack was to try doubling up some 0.021" Stainless Aircraft Safety Wire and see if it could be placed into the bolt's hex head cavity and have a slightly larger hex head socket drive (8mm to 1/4" hex tool) driven in with a brass hammer to increase the purchase of the hex tool to remove the stubborn stripped bolt.
I bent the safety wire using my needle nose pliers and formed this: (Note...the photo is the replaced bolt because it didn't take a photo before removal attempt. Only shown for wire placement example)
This fitted into the stripped bolt head like this:.
This was a photo of the concept attempt:
Followed by driving the 1/4" inch drive hex socket into the bolt hex head. It worked like a charm. No special tools or extractor required. Below is the actual extracted bolt.
I was a bit amazed at the ease of this hack. It required no special tools and theoretically could be performed in the field provided you could find appropriate wire to complete the task. This took about 30 minutes with some concept wire placements to figure out if this might work. Once I figured out a workable wire placement, it took only a few minutes. Cheers!