Thomson 410mm layback.jl said:Padre,
I've had no problems. What kind of seatpost are you using? Did you grease it?
Padre said:Thomson 410mm layback.
I used a ton of grease.
Apparently, according to Devin, some welds inside weren't cleaned up or something? He was willing to fix it or whatever but I didn't see the need..until now!
I'm "letting" the liquid wrench sit over night..but I sure hope there is light at the end of the tunnel...[/QUOte
OK I know this may sound extreme, but I work with alot of dissimilar metals in harsh environments...when I get in this situation I've found that a bit of heat from a propane torch gently and evenly applied will expand the outer metal enough to let the liquid wrench work it's magic. If you do it evenly and slowly it won't even mess up the paint or finish.
You're right! that DOES sound extreme...but one I'll be using as a "last resort," if it comes down to that....Tex Mannz said:OK I know this may sound extreme, but I work with alot of dissimilar metals in harsh environments...when I get in this situation I've found that a bit of heat from a propane torch gently and evenly applied will expand the outer metal enough to let the liquid wrench work it's magic. If you do it evenly and slowly it won't even mess up the paint or finish.
Tex Mannz OK I know this may sound extreme said:Maybe an ice pack wrapped around the exposed post while you heat the tube with a blow dryer...........it might work?!
You could always beat on it with a worthless old Sidi Shoe![]()
Tex Mannz said:I watched a guy set fire to his frame doing that.Padre said:OK I know this may sound extreme, but I work with alot of dissimilar metals in harsh environments...when I get in this situation I've found that a bit of heat from a propane torch gently and evenly applied will expand the outer metal enough to let the liquid wrench work it's magic. If you do it evenly and slowly it won't even mess up the paint or finish.
Soaked in penetrating oil! He was trying to remove a snapped and frozen post.Cloxxki said:Wooden frame, or magnesium? Or just really wet paint?![]()
20.100 FR said:put the frame upside down and fill the seat tube with lubricant
heat gently the frame with an hair dryer
cool the seatpost with a co2 cartridge
use a coin to push on the skrew of the fast release so that it opens wide.[/QUOT
This method should work. I would use ammonia instead of lubricant, sounds like there has been some galling, and you need to dissolve this metal/metal bonding as much as posssible, not just lubricate it. Take out the crank and bottom bracket, get a 2' long piece of wood clothes closet bar, wrap tape around it to make it about the same diameter as the bottom bracket With the frame hanging upside down and the seat post end plugged, fill the seat post/seat tube up with ammonia so that the whole post/tube intersection is submerged. Put the closet bar in the BB shell in a "T" fashion, put an old seat on the post. Put some tape around the top of the seat tube so the ammonia doesn't leak out. Wait three or four hours and then try twisting them apart again, takes two people unless you have the closet bar secured to something solid. If it doesn't work, wait 24 hours and try again. If it still doesn't work, wait another 24 hours. If it is still stuck, go get some dry ice. Unplug the seat tube, drain the ammonia, and then stuff dry ice chunks three to four inches up the seat post. Heat the seat tube with the hair drier. Twist. If this doesn't work, then you have to cut the post off with one inch left out of the seat tube, get a brand new triangular file and file a groove in the thin side of the post, CAREFULLY, until you are a paper thin distance from the seat tube. Drill a 3/8" hole in the seat post and put a 3/8 x 6 carriage bolt through it as a "T" handle and twist and pull. It WILL come out.Filing the groove is the only tedious part, and the only part that can hurt your frame. If you have a grinder, grind the end of the file to a blunt round point so the sharp edges at the end don't have any possibility of gouging the seat tube, or put some electrical tape around the end of the file. That is why I suggest a new file, it will take less time and you will get less frustrated.
I made a seat tube "hone" out of a wood dowel with 400 grit sand paper glued to it. Get a dowel that is smaller by 1/16" or more and wrap enough sand paper around it until it fits with minimal space, it needs to have little slop to keep from distorting the bore of the seat tube. Hone the seat tube once you have the post out.
lithiapark said:Call me lazy, but all this seems like too much work. FedEx that thing back to Devin it'll take about the same amount of time, save you grief and further aggravation, not to mention fixing the problem so it doesn't happen again.20.100 FR said:put the frame upside down and fill the seat tube with lubricant
heat gently the frame with an hair dryer
cool the seatpost with a co2 cartridge
use a coin to push on the skrew of the fast release so that it opens wide.[/QUOT
This method should work. I would use ammonia instead of lubricant, sounds like there has been some galling, and you need to dissolve this metal/metal bonding as much as posssible, not just lubricate it. Take out the crank and bottom bracket, get a 2' long piece of wood clothes closet bar, wrap tape around it to make it about the same diameter as the bottom bracket With the frame hanging upside down and the seat post end plugged, fill the seat post/seat tube up with ammonia so that the whole post/tube intersection is submerged. Put the closet bar in the BB shell in a "T" fashion, put an old seat on the post. Put some tape around the top of the seat tube so the ammonia doesn't leak out. Wait three or four hours and then try twisting them apart again, takes two people unless you have the closet bar secured to something solid. If it doesn't work, wait 24 hours and try again. If it still doesn't work, wait another 24 hours. If it is still stuck, go get some dry ice. Unplug the seat tube, drain the ammonia, and then stuff dry ice chunks three to four inches up the seat post. Heat the seat tube with the hair drier. Twist. If this doesn't work, then you have to cut the post off with one inch left out of the seat tube, get a brand new triangular file and file a groove in the thin side of the post, CAREFULLY, until you are a paper thin distance from the seat tube. Drill a 3/8" hole in the seat post and put a 3/8 x 6 carriage bolt through it as a "T" handle and twist and pull. It WILL come out.Filing the groove is the only tedious part, and the only part that can hurt your frame. If you have a grinder, grind the end of the file to a blunt round point so the sharp edges at the end don't have any possibility of gouging the seat tube, or put some electrical tape around the end of the file. That is why I suggest a new file, it will take less time and you will get less frustrated.
I made a seat tube "hone" out of a wood dowel with 400 grit sand paper glued to it. Get a dowel that is smaller by 1/16" or more and wrap enough sand paper around it until it fits with minimal space, it needs to have little slop to keep from distorting the bore of the seat tube. Hone the seat tube once you have the post out.
e
LOL!!! You're right, I just never thought of that. It strikes me as funny 'cause its true and I realize I never think about letting anyone else help me. Even if I don't know what I'm doing, I just charge ahead. Occaisionally when the problem is resolved, I recognize how much time I spent working on a problem instead of riding one of my other bikes and wish I'd made another choice (seems like there might be a metaphor for my life in here somewhere). But I learn a lot of interesting things along the way.escamillo said:Call me lazy, but all this seems like too much work. FedEx that thing back to Devin it'll take about the same amount of time, save you grief and further aggravation, not to mention fixing the problem so it doesn't happen again.
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